As you saw from part 1, the amplifiers were
to be converted into a fully working integrated
amplifier - this would be no mean feat.
Inputs
The design called for several audio
line inputs as per a regular audio pre-amp,
originally the only inputs were the microphone and
line inputs so that part needed completely
redesigning. Because of the location of the input
switch, relay switching was decided on for several
reasons – firstly because of the combined length of
the audio cables routing to a regular switch, but
also because space around the selector switch would
be tight and good quality selector switches tend to
be bulky, not to mention expensive.
By using relays to switch the audio inputs, the
signal lines are kept as short as possible, if well
designed there are substantially less issues with
crosstalk or connection problems as there might be
if inexpensive switches are used to switch the audio
signals themselves, also it's easier to ground the
unselected inputs to cut noise and crosstalk (normal
switches would need extra sets of terminals to do
just that). With this design, a simple, inexpensive
selector switch can be used because all it will ever
do is switch the +5v power supply feeding the relay
coils and the indicator lamps on the front panel. If
good quality signal relays are used, it will work as
well as any high quality audio selector switch
would. Inexpensive rotary switches are still
reasonably rugged and still feel positive to use,
there's no problem at all with using one.
Originally, I was going to build the circuit onto a
regular strip board but I wasn't happy about
building that amount of complexity without a regular
PCB layout, especially where low level signals were
involved – problems with crosstalk and noise could
easily become a problem. Besides, once you build
circuits onto the board they inevitably become a
mess, with even the best intentions the board layout
will most likely look awful by the time you've
finished with drilled or split tracks and wire links
all over the place. Besides, a professional finish
means a lot to me.
I designed the boards in Linux using KiCad, an open
source program which handles both the creation of
schematics and also the actual laying out of the PCB
itself. Even with a reasonable background in
computer design, KiCad isn't easy to get the hang of
but once you do, it's a solid program and it can
create professional looking board layouts. The thing
to remember about a program like KiCad is that it
forces you to be organised, you can't just go in and
start clicking around adding random components to
create a board. In KiCad you need to create a
schematic first and then assign all of those
components to case styles and footprints before you
even think about putting them onto the PCB – it's a
lot of planning but it pays off when you end up with
a professional looking board layout where all the
components fit well. Really, this amount of planning
only becomes worthwhile if you're planning a
production run of boards, where the time spent
planning everything out would reap rewards when you
could easily duplicate the boards without errors.
That said, it's still nice to have a professional
looking finished product, even if it is only a
one-off.
I developed the board the old tech way, using toner
transfer paper to get the track design on and then
etched in ferric chloride for an hour in a warm
place; I am seriously considering investing in the
equipment to etch UV sensitive boards, this is a
much more exact approach for anything more than a
basic prototype and you'd need that extra accuracy
if you were attempting complex board layouts. The
toner method takes some care and is no good if you
are trying to create a large number of boards, but
for single boards it can work well.

The etched and cleaned PCB, not drilled
yet. |
This was the first time I had
attempted prototyping circuit boards in a long time
and my first time designing them on computer,
overall it went very well. With hindsight, I could
have made the pads around some components larger and
I accidentally omitted the shunt diodes on the relay
coils (the result being a loud 'pop' sound through
the speakers every time the inputs were switched,
quite alarming until I realized my mistake) - these
were easily added in after, neatly soldered in on
the track side of the board. Apart from this,
everything went well and the circuit worked as
expected from the start.
To keep things as simple as possible, I decided to
keep everything to do with the audio inputs/outputs
and switching on the rear panel – this meant a rear
panel containing all the sockets (mains, line audio,
speaker) and attached to that the PCB which
contained the switching relays and also the
regulated 5v power supply to feed both them and the
LED source indicators on the front panel.
The power supply was originally to be taken from a
heater winding on the left channel's mains
transformer, the transformer had ample rating and
added to that the fact that the oscillator valve was
now removed allowed more than enough power to be
tapped from it. The 6.3v AC supply was originally to
be taken from the transformer on the left channel
amp and fed through a rectifier and +5v regulator
circuit (relays and LEDs all rated for 5v), I
eventually powered it from a small auxiliary
transformer which also powered the VU meters.

Rear panel assembled. This was more of a
prototype, afterwards I decided to change the
design and made a new chassis from aluminium |
Display
A display was to be fitted to show what input was
selected, this came from a donor amplifier of some
description. Originally using lamps, it contained 4
clear plastic panes with PHONO, TAPE, TUNER and
CD/AUX engraved onto them so that the lettering lit
up. High brightness LEDs worked well in place of
lamps - these were run from the selector switch in
parallel with the relays.

Input display. Red, white, green and amber
LEDs were fitted and held in place with high
tech putty otherwise known as Blu-Tak.. |
Chassis
The rear panel was originally to be made from some
black coated steel sheet I had spare, I decided to
change this for a full chassis because I wasn't
happy with the overall look and the prospect of all
the wiring being tugged about when it was all being
fitted into the case.
I changed the design and made a new
complete chassis from a combination of 1.2mm
aluminium sheet and 1.5mm aluminium profiles,
designing and building something like this from
scratch with hand tools is no easy task but with
care the finished product can be good. Smaller holes
were drilled using engineering grade twist drills
(buying a kit of good engineering drills gives you a
LOT of sizes to choose from), the larger holes were
punched for neatness - try drilling anything larger
than 8mm through metal sheet and you're asking for
trouble.
However, punches are only available
to cut down to 10mm or so, hence there's no
alternative but to drill the smaller holes manually.
I planned the panel out in a 2D CAD program and then
exported the plan to a regular graphics program to
add the lettering and logos, these were then
converted to negative, mirrored and printed onto
transfer sheet and applied to the prepared metal
panel using heat and lots of pressure. The large 'A'
logo was the original circa 1960's Akai logo, copied
from the nameplate on the front panel of the tape
unit and reproduced as a vector image in Paint Shop.
The Briarsfield logo was added at the request of my
customer, it wasn't my idea.
The grille was added for obvious
reasons, that was a steel mesh which was primed and
sprayed anthracite - I bowed it slightly to make it
fit tight against the rear panel so it wouldn't
rattle.
Once cut and drilled, the panel was wet sanded to
produce a brushed finish and once the lettering had
been applied it was then lacquered, this lacquer
then wet sanded until relatively smooth and finally
polished, like a pseudo clear anodized finish.
The lettering was experimental, this was difficult
to make work and although the result wasn't perfect,
I was still quite pleased with it - silk screening
would have been the ideal but that takes a large
amount of money and investment in equipment, only
worthwhile if you had the space and enough use for
it. The problems I had here were from the heat
necessary to make the print stick to the metal, the
metal expanded slightly more than the printing and
hence smudged the lettering in places. Really, this
was a test to see whether I could get something
approaching a professional finish using basic
materials.



Rear section of
chassis assembled. A totally huge amount
of work to get this level of finish.
|
VU meters
The amplifiers originally had VU meters fitted,
these were powered from the loudspeaker output and
were each fitted with a pair of 6.3v lamps, which
were powered by one of the valve heater windings on
the transformer. The design called for the lamps on
these to be fitted with a combined dimmer and on/off
switch and for the meters themselves to be powered
from the signal circuits in the pre-amp section of
the amplifier instead of the loudspeaker output as
they were originally. The dimmer circuit for the
lamps was simple enough, the original lamps were all
blackened with age so were replaced with miniature
screw cap lamps, 6.3v/150ma each. The dimmer circuit
was built from an LM317 adjustable voltage
regulator, the circuit configured to provide 6.25v
across the lamps when at maximum. This circuit also
needed its own rectifier to provide a DC supply
suitable for the dimmer module. The regulator itself
was fitted to the metal chassis to help keep it cool
(acting as a large, conveniently placed heatsink) –
however, as the metal tab on the LM317 is connected
to the voltage output, it needs to be electrically
insulated from the chassis while still being
connected thermally.
Driving the meters themselves from the existing
audio circuitry was a challenge, under test they
needed around 2.8v to drive them into the +3dB red
band – no part of the existing audio circuitry could
provide this amount of voltage swing. I decided to
power them from dedicated op-amps, these would take
a voltage from any point of the audio circuitry that
I chose and amplify it enough to power the meter.
The idea here being that an op-amp has a very high
impedance input and hence copies the signal which
you feed into it but doesn't place any load that
signal, it has virtually no negative effect on the
audio circuitry at all.
I tried several different circuits, in the end it
became clear that I needed to build a complete
miniature amplifier for each meter complete with
gain control and power supply to make everything
work well. The circuit was a non-inverting type
op-amp with a maximum gain of 10, I chose
non-inverting because I was concerned about any load
being placed on the audio circuitry. The op-amp used
was nothing special, merely an LM741 – easily good
enough to drive the meters. The inputs and outputs
were DC coupled and the power supply on each one
included a rectifier and a pair of 330µF capacitors,
the value of these being certainly more than enough
to provide smooth, stable voltage rails to drive the
meters.
Originally I was intending to build the circuits
onto a custom designed PCB as I had with the input
board. However, I built the test version onto tripad
board and altered it several times; at that point it
worked well, was the right size and looked
relatively neat so I left it alone – designing,
developing and cutting a custom PCB would have added
a great deal of extra work for no gain.
I originally planned to power the VU's from the
heater windings, in practice this caused some
problems with noise and also the lack of voltage
available and also the lack of a centre tap caused
its own issues with DC offset and bias - the bias at
least would be easy to correct but would still leave
little voltage swing, the 6.3v from the heaters
being enough in theory to push the meters into their
red bands but in practice a small separate
transformer with 2 x 6v windings being much better.
The amplifier boards were fixed to the back of each
VU meter. I fused both sides of the AC line for
safety, again this is overkill from a design
perspective but it doesn't hurt anything.

Photo of one channel's VU amplifier. Blue
trim pot is for gain. Lots of wiring in there
now, starting to get cramped.. |
Tone controls
The design also called for a set of
tone controls to be fitted. This proved a conundrum
to me, after I had agreed to design them in and sat
down to do the math, it was clear that things
weren't going to add up together without some
changes elsewhere. The problem with tone controls in
valve equipment is that they're often passive and
sit inline with the audio signal between two stages.
Nothing wrong with this approach at all but
inevitably you'll lose a large amount of gain as the
controls can only provide a loss of volume level, at
least if you were designing an active network you'd
usually sit it in some kind of local feedback
network and you'd add an extra valve or transistor
stage, correcting any gain you would lose in the
first place.
I built the circuits on part of the
main tag board on each channel which had been
cleared of components during the upgrade. As they
would only ever see around a volt of signal, 1/4
watt metal film resistors and LCR polystyrene
capacitors worked well. The actual tone pots aren't
anything special, merely 250kohm Alpha guitar pots.
The results of the first test after
the controls were fitted was predictable, what sound
was there was good and the tone controls worked as
expected but the volume level had been severely cut
- after all, the tone circuits were consuming over
20dB right across the audio spectrum when at their
neutral positions and that's a heck of a lot of
signal voltage to lose - you're effectively dividing
the input signal by 10. After reverse-engineering
each stage of the ECC83 the old fashioned way with a
loadline plotted on paper, it was clear from this
that each stage was already giving a gain of between
60 and 70 and squeezing any more from them would be
extremely difficult, especially on the existing 250v
HT supply.
Instead, I had a lucky break - it
seemed that the first ECC83 stage would be able to
handle around 1.2v of input before saturating, by
removing 20dB of cut from the attenuation networks
for the line inputs, I was able to compensate but
still keep the signal levels comfortably below this
threshold. This wasn't the perfect solution and I
realized that I was pushing the first ECC83 stage
pretty hard regarding sonics, but the extra gain did
help things a great deal. This change in design
meant that the tone switch would need to be fitted
with a -20dB attenuator on the tone defeat position
to match the volume levels, but that was easy enough
to modify.

Basic tone response, plotted in 5Spice.
This is theory, other factors will cause
roll-off at either end. |
Pre-outs
Another good thing with simple valve
amplifiers is that the final signal which goes to
the EL84 amplifier valve could just as easily be run
through a basic DC filter network to instead drive a
separate power amplifier. This isn't the ideal
solution, as valves like high impedance and most
power amplifier inputs will load the preceding stage
to somewhere around 50K ohm, fine for transistors
but far too low for valves to work comfortably with.
In practice it worked well, some slight compression
towards the lower bass but the sound was good.
The internal amplifier is reasonable
quality, compared to the average 'consumer grade'
transistor amplifier, it does compare well at low
listening levels, especially on vocal or acoustic
music - good components and clean signal path help
greatly with this but the amplifier still has a
large part to play in the sound. Power outputs
matter more to transistors than they do to valves, a
5 watt transistor amp would sound pretty pathetic
even if built with good components - many valve
supporters
say that 1 watt of valve power equals at least 2
watts of transistor power and that the first watt is
the part of the power spectrum which matters most.
However, our 5 watts still isn't a
great deal of power, although single ended
undoubtedly has a nice low/mid region for low to mid
volumes and ours had a very nice low end despite the
small output transformers. That power doesn't go
very far and even though you won't notice hard
clipping like you would with transistors, you'll
soon notice the lower frequencies start to bottom
out and lag and a hint of ringing as the volume
level increases. Still, for close listening at
normal low/mid volume levels they could handle a
pair of 8 ohm floorstanders with aplomb, this is
where they really shine.
I took the pre-outs from the final ECC83 stage,
before the coupling capacitor to the EL84 output.
Under test, this output would easily peak 1v at full
volume, more than enough to drive the average power
amplifier.
Originally, the EL84 power amp
section was to be switchable, so they could be used
as pre-amps driving an external power amplifier.
This caused several problems, firstly working out a
way to switch both HT supplies, both heaters and
both audio grid inputs. Finding a suitable switch
off-the-shelf for all these purposes would be near
impossible, relays would be ideal but then there's
the question of space (which was already starting to
become limited). Also I was worried about possible
problems in the event of one HT relay failing for
some reason but leaving the other HT feed powered,
this could cause some serious heat damage.
Also, the mains transformers are
quite small and small transformers inherently have
poor regulation. Once the current draw for the EL84
was removed, the HT voltages would inevitably shoot
up dramatically - from around 260v to 370v - this
could have been explosive if the original 350v power
supply filter caps were used, luckily the new ones
were rated at 450v and could handle this extra
voltage, but it's worth considering. This extra HT
voltage would also add more gain, all of this
combined with the removal of the EL84's negative
feedback network would add another 25dB of gain
which would send volume levels far too high and
cause very audible problems with microphony and
compression between the two ECC83 stages.
Between the loudspeaker sockets was
fitted a push switch to switch the loudspeakers on
and off. With the switch in the 'off' position, the
speaker outputs are disconnected and the amplifier
is run through a dummy 8 ohm load - you need this to
keep the correct frequency response if running as a
pre-amp or using headphones. This switch was the
original record/monitor switch, it was open chassis
so could easily handle a couple of watts. It was
fitted to an aluminium bracket and screwed to the
rear panel with spacers.
Curiously, the pre-out filter
capacitor is one of the largest components in the
amplifier, even though it's relatively small in
value. Even if I wanted to, I couldn't use an
electrolytic here as we're running the pre-outs from
the second ECC83 stage anode, which runs at around
125 volts relative to ground - the average audio
grade electrolytic normally used for DC audio
coupling would explode at these voltages, allowing
the 125v anode voltage across the inputs of the
connected power amplifier - something I assure you
would not be a nice experience. This is a normal
2.2uF/400v polypropylene capacitor, virtually the
same component that you would find inside a good
pair of speakers, used here to filter out the DC and
give us the low sub-20Hz cut-off frequency which
we've tried to maintain through the rest of the
amplifier.
This isn't ideal, usually it's
advisable to keep impedances higher and use smaller
capacitors as smaller capacitors are regarded as
more perfect - alas, real life isn't this simple and
as the majority of (transistor) power amplifiers are
between 47k and 100k input impedance, we've no
choice but to use a relatively large coupling
capacitor in an effort to keep the low frequency
roll-off below 20Hz.
On to part 4